Have you encountered difficulties setting a plug in a high deviation well?
If so, Peak can help.
We assisted a National Oil Company in Brunei set their 3-1/2" SIM Plug (nippleless plug) using mechanical slickline in order to isolate a failed inflow valve in a high devation gas well. The object of the exercise for the Customer was to evaluate the reservoir data as justification for future stimulation.
Three third-party formation isolation valves had previously failed and could not be used as a means of isolating the producing sands. The deeper deviated section of the well had also proved problematic in earlier well intervention operations, where the tubing crossover from 4-1/2" to 3-1/2" tubing was located.
Peak's solution provided many benefits to the Customer.
To find out more, download the case study in full by clicking the link below.
If you are encountering similar challenges, we are here to help. Please contact us to speak to one of our Technical Sales Managers to discuss your requirements further.
Product Code(s): SIM Retrievable Bridge Plug - 351; SIM Running Tool - 350
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