Peak Well Systems Blog

Retrieval of injection valve from tubing crossover at depth

Posted by Peak Well Systems on 05-Jul-2016 12:30:00

A Customer was retrieving a bridge plug and injection valve to surface when the injection valve separated from the plug and landed at the 5-1/2" by 4-1/2" tubing crossover at 10,400ft.

An efficient method to fish the injection valve without causing damage to the tubing crossover was required so the injection value could be pulled and a new injection valve set.

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Topics: Technical Case Studies, Wellbore Clean-up and Debris Removal, HTHS Magnet

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